# HG changeset patch # User Jan Mulder # Date 1554716953 -7200 # Node ID 625d200702612de1a4e6c85993e0b53bafab13de # Parent e4207f0aaa4ba84425c530c9409e47f117297748 Improvement SPI stability/recoverability The core part of this commit comes from careful code reading. The core is the swap of Scheduler_Request_sync_with_SPI(SPI_SYNC_METHOD_SOFT) and SPI_Start_single_TxRx_with_Master(). This code is sitting in an if-clause that is triggered on SPI comms failure. Instead of blindly trying to communicate again (which will very likely fail again), first try to reset the comms link, and then try to communicate again. That simply makes more sense in this case. This is heavily tested, on 2 simple dives, and 5 very long deco schedules from the simulator (10+ hour deco's), and a lot of small simulated dives (upto 2h runtime). Of all these tests, only one long session failed after 9 out of 11h runtime. Analyzing that one failure, suggests that the RTE is looping in some error handler, which (obviously) results in a SPI comms failure as a result. I consider this not part of this change. Additionally, some more cleanup is done in this code. Signed-off-by: Jan Mulder diff -r e4207f0aaa4b -r 625d20070261 Small_CPU/Src/scheduler.c --- a/Small_CPU/Src/scheduler.c Mon Apr 08 10:35:29 2019 +0200 +++ b/Small_CPU/Src/scheduler.c Mon Apr 08 11:49:13 2019 +0200 @@ -48,10 +48,6 @@ /* Private types -------------------------------------------------------------*/ const SGas Air = {79,0,0,0,0}; -uint8_t testarrayindex = 0; -uint32_t testarray[256]; -uint32_t testarrayMain[256]; - /* Exported variables --------------------------------------------------------*/ SGlobal global; SDevice DeviceDataFlash; @@ -121,7 +117,7 @@ global.ButtonPICdata[2] = 0xFF; global.ButtonPICdata[3] = 0xFF; - global.I2C_SystemStatus = 0xFF; // 0x00 would be everything working + global.I2C_SystemStatus = HAL_ERROR; // 0x00 would be everything working global.lifeData.pressure_ambient_bar = INVALID_PREASURE_VALUE; global.lifeData.pressure_surface_bar = INVALID_PREASURE_VALUE; @@ -415,8 +411,8 @@ /* Try to start communication again. If exchange is stuck during execution for some reason the TX will be aborted by the * function error handler */ + Scheduler_Request_sync_with_SPI(SPI_SYNC_METHOD_SOFT); SPI_Start_single_TxRx_with_Master(); - Scheduler_Request_sync_with_SPI(SPI_SYNC_METHOD_SOFT); } } @@ -437,10 +433,8 @@ float lastPressure_bar = 0.0f; global.dataSendToMaster.mode = MODE_DIVE; global.deviceDataSendToMaster.mode = MODE_DIVE; - //uint16_t counterSecondsShallowDepth = 0; uint8_t counter_exit = 0; - Scheduler.tickstart = HAL_GetTick() - 1000; Scheduler.counterSPIdata100msec = 0; Scheduler.counterCompass100msec = 0; Scheduler.counterPressure100msec = 0; @@ -451,6 +445,7 @@ scheduleSetDate(&global.deviceData.diveCycles); global.lifeData.counterSecondsShallowDepth = 0; + Scheduler.tickstart = HAL_GetTick(); while(global.mode == MODE_DIVE) { schedule_check_resync(); @@ -1335,8 +1330,7 @@ //Supports threadsave copying!!! void copyPressureData(void) { - global.dataSendToMaster.sensorErrors = I2C1_Status(); - //uint8_t dataSendToMaster. + global.dataSendToMaster.sensorErrors = global.I2C_SystemStatus; uint8_t boolPressureData = !global.dataSendToMaster.boolPressureData; global.dataSendToMaster.data[boolPressureData].temperature = get_temperature(); global.dataSendToMaster.data[boolPressureData].pressure_mbar = get_pressure_mbar();